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CJ750 toolbox |
Another piston meltdown
This one came out of the blue. The oil level was good,
the temperature was low, and the bike was loping happily
along around 45 mph. The engine suddenly started to
behave as if the rotor had come loose or the points were
closing up, so I pulled over and took a look under the
distributor cap. All was well. Being but a couple miles
from home, I decided to nurse the bike back to my garage.
Initially, it seemed like everything was going to be
fine, and whatever was wrong would be quickly sorted once
we were home. However, the engine ran progressively
rougher and with progressively less power. It was pretty
obvious that something serious was happening, so I
stopped and called AAA for a rollback. Once home, I
started tearing things apart. |
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This might explain why the bike was so easy
to kick overzero
compression on the port jug. The cylinder got damaged
too, as did the connecting rod, so this is pretty major.
(The starboard side is fine!) |
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Q: Here's what was in the
sump, but it accounts for maybe 20% of the missing
piston. Where did the rest of it go?! |
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A: It was lying on the
screen inside the crankcase. |
I'm gonna replace the whole motor this time,
and thanks to Jimbo, that is indeed on
the agenda.
Meanwhile, I'm trying to find the reason this happened.
With the previous incident, certain elements were present
(straight pipes with undersized jets, running too fast
for too long on a hot day, and not recognizing the
warning signs.) This time, things were a lot different.
I'm running 094 jets with proper fishtails, plenty of
fresh SAE40 oil, and most importantly, I was just taking
it easy on a nice cool day. Possibilities? Since this motor is equipped
with a deep sump and a high-capacity oil pump with
extended pick-up, lubrication has never been a problem.
My gut feeling is that the pistons were simply junk.
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